Well, we didn't break any thing :- But lots of WTF!!
1st pass 263 at the 21/4 not running right Troy shut down,
Back in pit, motor missing and popping, data showed low batteries, bought new, same bad MSD box, borrowed extra from Brian Dean the Thunder salt team, same. Finally found loose manifold bolts.We removed head after high EGT in $5 cyl at EL Mirage to check for damage, none. put back together, ran great tightened the hell out of manifold bolts only 5/16th wrench. We always retighten after first start up but we forgot to. Any how sitting in shade having a beer, I told my Grandson [driver next year] to remind us to tighten manifold bolts next morning about that time troy arrives from a few Pits over and one of the crew chies said to check for manifold leaks.
Troy says I'll tighten them right now.
Started up ran GREAT
Ran the next morning 273 + in the 21/4 273 ++ in the 3 Troy had his phone on GPS showing
286 at one point so pushed it hoping for a record but missed by just a few Hundreds.
Car stared off good 280 is our best 21/4 time but stayed flat.
Burned of sparkplug strap on that run in #7 and compression gauge showed no compression.
Turns out after showing normal compression on #1 #3 and#5 the gauge stopped working.
Maybe a good thing because we might not have removed head and piston. Bearing weird looking
piston OK no stuck rings, changed all rod bearings Put it together, fired up missing and popping
water in header #5 and #8
Thats, it DONE.
jl222
PS our 263mph run on 8- 3 was not listed in the results?